This problem did not get resolved until 2012. When motoring above about 2000 RPM the boat
would vibrate enough to be worrisome. My previous boats had resonances at different RPMs and
I would try to run at speeds that avoided the worst vibration. Applied Physics had what seemed to be similar vibration, only worse.
Edwin Muth suggested this level of vibration was not normal and he helped me try various fixes.
We carefully aligned the shaft, but it made no difference. I also installed an R and D shaft coupling, but it did not help.
Before the 2011 season, Lockwood Boatworks suggested the problem was the Maxprop, which they sent back to PYI for reconditioning.
PYI said the prop had a crack which they repaired. They also reconditioned the prop. Nevertheless, I still had most of the vibration.
Early in the 2012 season Robert Lockwood went for a test ride with me and decided that the prop was probably still bad.
This time I ordered a new prop which Robert installed. For the first time my boat ran without vibration.
Also, although the settings on the new Maxprop were the same as the old,
now I got 7 knots at 2000 RPM as opposed to 6 knots at 2000 RPM with the old prop.
Either the new Maxprop was redesigned or the old one was fundmentally flawed.
Furlboom Boom Furler
We ordered our boat with in-boom furling. We did this for the follwing reasons:
The boom on the Hunter 44 is too high to allow convenient standard flaking with
someone of my height (5'10")
Vertical battens were unproven technology in 2004 when we order the boat
We were leery of in-mast furling because of the poor sail shape it provides and
because of the fear that if the sail jammed in the mast we would not be able to
lower the main in an emergency. With in-boom furling, even if the sail jams in
the boom, the sail can still be lowered.
We
soon found that our furling system, as installed, was not easy to use. Cranking
in the last 10 feet of the mainsail was difficult ... it seemed that there was
too much sailcloth for the diameter of the boom and the sail was being forced
into too small a space near the gooseneck. In addition, because of the tight
fit, it was very hard to pull the covering flap across the top of the boom to
protect the sail when it was furled. But most troubling of all, the bolt rope
on the luff tended to move past the forward end of the furling mandrill and
jammed against the gooseneck. This was compounded by the battens moving forward
past the bolt rope.
The bottom photo of the pair shows the as-delivered system partially furled.
Note how the batten has moved forward. If furling were to continue, the cloth
would start to jam into the gooseneck.
We made numerous calls, first to our dealer, Sandy Hook Yacht Sails, then to
Furlboom, who instructed us to adjust the angle between the boom and the mast
and to be sure to apply enough tension to the halyard as the sail was furled.
None of this worked. We struggled with this system for two seasons when I
finally e-mailed the lower image to Dougall Johnson at Furlboom. He immediatly
saw that the sail was not made to Furlboom's specs. First, the bolt rope was
too large, and second the batten pockets were not properly formed. Hunter had
supplied the sail, which was made by Doyle. I called Doyle and they said the
problem was my fault because I wasn't using the system properly. Hunter stepped
in and arranged for my local sail loft, John Eggers, in Sayerville, NJ to
modify the sail with Hunter footing the bill. Dave Thompson from Eggers met
with Dougall at the Annapolis boat show in the fall of 2006 and discussed how
the sail need to be changed. Dave did the work, and the result is shown in the
top photo. The boom angle still matters and there still needs to be tension on
the halyard when furling, but it is not magic. Now the covering flap fits
better, and there is enough space in the boom for the sail because the bolt
rope is no longer too fat. Hunter came through, Furlboom was helpful, Eggers,
as usual did a great job, but Doyle was worse than useless.
Macerator Wouldn't Suck
Being out on the ocean and not being able to dump the poop is not fun. Just
after a month of use, we found the macerator would not pump out the holding
tank in the usual way. Being one to follow the rules, I could only test this
sytem when I was three miles offshore, usually in a swell. I had found that I
could prime the pump and make it work by closing off the holding tank vent and
then presurizing the tank with an air bellows pump through the pumpout
deckplate while the macerator was being run. This required three people: one to
hold the macerator switch, one to run the bellows, and one to look at the stern
to confirm that the macerator was actually pumping.
After our 2005 cruise, Kevin McGettigan, our dealer from
Sandy Hook Yacht Sales, made a trip to our boat at its Keyport mooring and
disassembled the system and found that the macerator did indeed pump. ( I had
emptied the holding tank at a pumpout station, but it was still a nasty job for
Kevin.) But the next time we were three miles offshore, we still could not get
the macerator to pump. I called Hunter and they sent me a new pump, which I
then had the pleasure of installing. Still no good.
After much thought, I decided that the most probable cause was too little
clearance between the bottom of the macerator intake tube and the bottom of the
tank. If there were just enough gunk at the bottom of the tank, there would be
too much resistance to flow at the gap between the tube and the tank: the pump
would not be able would be able to self-prime. I pumped and flushed the tank
real well, and then removed the tube and sawed off about 1/2 inch of the PVC
tube. I did this job in early spring, so the system was cold and had little
fragrence. The reassembled system has been working for two years.
Engine Ran Hot
At the beginning of the 2006 cruise, just after passing Montauk, Dan Musgrove
noticed that the engine temperture was running hotter than had been typical,
which was just below 80C. We had been motor sailing at about 2500 rpm. As we
got to colder water the temperature dropped and I stopped worrying about it. On
the way back from Maine, as we returned to warmer water, unless I kept the rpm
below about 2200, the engine temperature rose well over 80C. I thought perhaps
we had barnacles on the prop and I hired a diver to scrape the bottom in
Vineyard Haven, but it made no difference. I also had a Yanmar tech check out
the engine thermostat in Newport, but everything was declared to be normal.
Back at Keyport a mechanic again looked at the engine, and suggested replacing
the temperture gauge. I did this, but new gauge also registered "hot".
Mastry, Yanmar's distributor in Florida, suggested that I try cleaning the
cooling system with Prestone Radiator Flush on the theory that gunk was
deposited on the heat exchanger tubes. This turned out to be a tedious, messy
job, but the engine ran cool for another season, and then the problems started
again. I flushed the heat exchangers again in the summer of 2007 at a mooring
in Rockland, Maine and got some relief, but to do the job right, at the end of
the 2007 season, Mike Lockwood at Lockwood Boatworks pulled out the heat
exchanger tubes and soaked them in an acid bath. Last year I had no trouble at
all. Somehow the original engine coolant broke down and coated the tubes. My
plan is to now change the coolant every season.
Tachometer quit when the battery was fully charged
As delivered, the tachometer was setup to run off the alternator. But the
alternator on Applied Physics is controlled by a Link 2000R smart voltage
regulator. When the batteries are nearly fully charged, the voltage regulator
tells the alternator to stop putting out current so there is no longer a signal
for the tachometer to read. Kevin McGettigan at Sandy Hook resolved the problem
by having a traditional magnetic pickup installed on the flywheel to send a
signal to the tach. The amazing thing was that Yanmar and Hunter said we were
the first to report this problem.
No Manual Recovery on Anchor Windlass
This problem is not resolved. The Simpson Lawrence, Sprint Atlantic Windlass,
that came with our boat, has no provision for manual recovery. This means that
if the power fails, there is no good way to haul up the anchor. We have 120
feet of chain rode, and hauling in the rode by hand without mechanical assist
does not seem possible. I have talked to Lewmar, who now supplies this
windlass, and after delays and a runaround, and my expressed willingness to pay
for an upgrade, I was ignored. Lewmar claims they never had one of these
windlasses fail. I am glad they are so confident in their product and that they
are sure that I will always have electrical power on my boat in an emergency.
Hunter wasn't much help either.
Raymarine autopilot clutch failed to engage when boat was
healed on starboard tack
This problem appeared after the third season and continued to
worsen. Even though I was convinced the probelm was limited to the drive unit,
Raymarine said they would attempt a repair only if I sent all components
of the autopilot system to them, an offer I could refuse. Buying a new unit
would have cost about $1K, so during the winter of 2006 I decided to try to fix
the drive unit myself. In taking the drive apart, I discovered the clutch
mechanism is very simple: it is just a solenoid that stops a freewheeling disk
(part of a differential drive) allowing the motor to move the linear drive. The
freewheeling disk is a magnetically susceptible material that closes the
magnetic circuit between the poles of the solenoid.
When the boat is heeling on a starboard tack, the solenoid has to move "uphill"
to reach the clutch disk. When there was too much tilt, the solenoid could
not fight gravity. (I confirmed this on a bench test using two lantern
batteries to drive the solenoid.) My best guess is that the clutch had worn
down over time, increasing the gap between the solenoid and itself, so that the
magnetic field of the energized solenoid was too weak to overcome the
combination of gravity and the solenoid spring. I shimmed it with a 10
cent washer, and in sea trials in June 2006, it worked fine.
Backlighting on breaker panel labels failed
The labels are lit by an electroluminescent fiber that
sometimes shorts at its far end. To fix the fiber I followed this procedure:
"Turn off the power to the panel lights, carefully remove the foil at the tail
end of the fiber, and then take a single edge razor blade and trim about 1/8"
from the end of the fiber. There is probably a short at this point that has
caused the problem. Tape over the end of the fiber with insulator and
you are likely good to go." I got this tip from the maker of the fiber who I
traced down from leads that I got from Hunter several years ago.
Other stuff that broke
My friend, Edwin, said a few weeks ago ( May 2010) that few
things ever broke underway on his boat. I have not been so lucky.
Here is a partial list of annoying failures not listed above:
1) Boom vang fell off the boom just south of the
GW bridge - a cotter pin failed. Fortunately conditions were calm and my
strong friend, Jerry Vogel was onboard, so we were able to use the topping lift
to reposition the boom and reinstall the vang. (2008)
2) Pressure water pump failed - easily replaced (2008)
3) Alternator failed - returning from summer cruise -
replaced in Gloucester- I now carry a spare. (2008)
4) Bow thruster failed - start of summer cruise - gear box
replaced - required a short haul in Newport RI. The failure also blew a 200A
fuse. Now I carry spares. (2008)
5) Raymarine E80 nav station unit died - unit sent
back for repair - cost ~$700. The old wiring had the radar and AIS
signals terminate at an E-80 at the nav station, so if the nav
station unit failed, radar and AIS info was not available at the cockpit
E-80 (I have two units). In addition, If the cockpit unit failed, the one
in the nav station could not be moved to the cockpit and achieve full
function. I had wiring changed so that radar and AIS now terminate in the
cockpit. (2009)
6) At the end of a cruise to Maine, I noticed that there
were machine nuts on the swim platform. The bolts that hold the
quadrant to the rudder had come off and the rudder stock was only held in place
by a small cotter pin. The rudder was wobbling around. I retightened
the bolts with Locktite. (2007)
7) Cockpit light constantly goes out - the connection
corrodes. Every season it needs to be taken apart and jiggled.
8) Wheel fell off at the mooring in a Nor'easter. Now
we tie down the wheel before a forecast storm. (2005)
9) The anchor roller was bent by the mooring chain in a
Nor'easter. (2005) We had two snubber lines as a bridle, but one broke in
the storm, and full force of wave was on chain which was led through the
roller. Since then we switched to dual polydyne lines and have had no
problems.
10) Rudder angle sensor detached from linkage. This has
happened more than once. The cockpit floor has to be opened to fix. I
tapped it on fairly tight last time. It has not failed for several seasons.
11) Yanmar engine hour counter display failed. This is
part of the tachometer. I wired in a stand-alone hour meter.
Fortunately this occurred at about 1000 hours, so the bookkeeping is easy.
12) Halon fire extinguisher in engine room emptied during
winter (2008). I was unaware of the interlock between the pressure gauge
on the extinguisher and the Yanmar engine. Mike Lockwood found the
override switch so I could start the boating season while a new extinguisher
was ordered.
13) Weight of winter cover knocked down stantions
(2006). We discovered that backing washers were not alligned with
bolts that held stantions in place - this was during construction in Florida.
New washers were added. We also added large backing plates under the main bow
cleats.
14) Shower sump pump failed - replaced. (2008)
15) Solar cell voltage regulator failed -replaced. ( 2008)